1
0
Fork 0
mirror of https://github.com/betaflight/betaflight.git synced 2025-07-24 00:35:39 +03:00

removed MAP_TO_SERVO_OUTPUT on PWM8/9

probably it fixed #1129
This commit is contained in:
TheAngularity 2016-09-09 10:25:48 +02:00 committed by GitHub
parent cab7b562d8
commit c595a789fc

View file

@ -30,8 +30,8 @@ const uint16_t multiPPM[] = {
PWM5 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM6 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM7 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM8 | (MAP_TO_SERVO_OUTPUT << 8),
PWM9 | (MAP_TO_SERVO_OUTPUT << 8),
PWM8 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM9 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM10 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM11 | (MAP_TO_MOTOR_OUTPUT << 8),
0xFFFF
@ -44,8 +44,8 @@ const uint16_t multiPWM[] = {
PWM5 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM6 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM7 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM8 | (MAP_TO_SERVO_OUTPUT << 8),
PWM9 | (MAP_TO_SERVO_OUTPUT << 8),
PWM8 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM9 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM10 | (MAP_TO_MOTOR_OUTPUT << 8),
PWM11 | (MAP_TO_MOTOR_OUTPUT << 8),
0xFFFF